February 25, 1992 - Philadelphia Electric agreed to pay
$285,000 in fines for the improper insulation of safety system
relief valves at Unit 3. Company spokesman Neil McDermott admitted
there is "absolutely no question and we readily admit that the insulation
was improperly installed" (Patriot News, February 25, 1992.)
March 6, 1992 - The NRC observed: "Several weaknesses were
noted in the training program during the conduct of the examinations.
Differences between Peach Bottom and Limerick had a negative impact on
some LSRO lesson plans in that the lesson plans did not track actual plant
practice. LSRO responsibilities were not well defined at Limerick and differ
from those at Peach Bottom. Training was not always given as described in
the task to training matrix or the qualification manual. In general, the
candidates' knowledge of the site and plant at which they were not
normally stationed was weak." (Lee H. Bettenhausen, Chief, Operations
Branch, Division of Reactor Safety.)
March 10, 1992 - PECO "concluded" that Units 2 & 3 had
deficiencies in their primary containment isolation systems.(NRC
inspections 50-277/92-07 and 50-278/92-07.) (See December 16, 1991
for related incident.)
March 10, 1992 - The NRC's Integrated Performance Assessment
Team (IPAT) observed, "an operator exit the fourth floor administration
building radiological control point...without properly surveying personal
articles being removed from the radiological control area" (NRC Region I
IPAT 50-277/92-80 and 50-278/92-80.)
March 13, 1992 - Philadelphia Electric "discovered" Unit 2 residual
heat removal equipment valves were not installed."With the check valves
on the discharge of the sump pumps for the 'B' and 'D' RHR rooms not
installed, this design basis can not be met. Specifically, during a loss of
coolant accident, concurrent with a loss of off-site power, the reactor
building sump pumps would not be available due to the loss of off-site
power" (NRC inspections 50-277/92-07 and 50-278/92-07.)
March 16, 1992 - Due to a turbine exhaust drain line valve failure,
the Unit 2 high pressure coolant injection system was rendered
inoperable.(NRC inspections 50-277/92-07 and 50-278/92-07.) (See
March 23, 1992 for related incident.)
March 23, 1992 - PECO "declared the HPCI system inoperable
when the turbine overspeed trip device did not reset during testing" (NRC
inspections 50-277/92-07 and 50-278/92-07.) (See March 16, 1992 for
related incident.)
March 26, 1992 - PECO "declared all Unit 2 reactor water level
instrumentation associated with the 2B reactor water level reference leg
condensing chamber inoperable" (NRC IR 50-277/92-13 and 50-278/92-
13.) (See September 11, 1990, March 27, 1992 and July 26, 1992 for
related incidents.)
March 27, 1992 - Unit 2 was shutdown due to inoperable reactor
level instrumentation. (See September 11, 1990, March 26, 1992 and
July 26, 1992 for related incidents.)
April 2, 1992 - A settlement was announced on the two lawsuits
brought against PECO by Peach Bottom's co-owners: Public Service Electric
and Gas Company, Delmarva Power and Light Company and Atlantic City
Electric Company. The suits were related to the NRC shutdown of Peach
Bottom on March 31, 1987."As part of the settlement, Philadelphia
Electric will pay $130,985,000 on October 1, 1992 to resolve all
pending litigation." (Joseph Paquette, April 8, 1982.) (See July 27,
1988 for background material.)
April 7, 1992 - PECO began a planned shutdown for Unit 2 from
about 100% power. "The shutdown was required because a one inch vent
line failed at a welded connection on the condensate supply herder to the
offgas recombiner condenser...A reactor scram and primary containment
isolation system (PCIS) group II and III occurred" (NRC IR 50-277/92-09
and 50-278/92-09.)
April 17, 1992 - The NRC issued a Notice of Violation for the
following infractions: "Contrary to the above requirements, the ODCM
[Offsite Dose Calculation Manual] specified composite water sampler at the
intake had been inoperable during the period August 30, 1991 to March
19, 1992, and the specified composite water sampler at the discharge had
been inoperable since August 8, 1991 and remains inoperable at the time
this inspection [was] conducted March 23-27, 1992. The licensee's efforts
to complete corrective action prior to the next sampling period were
ineffective" (NRC inspections 50-277/92-08 and 50-278/92-08.)
April 29, 1992 - A Health Physics technician was contaminated
in the de-watering facility when "contamination controls were
compromised. According to the licensee's investigation, a defective latch
and hinge on the fill-head access door allowed contamination to escape
from the liner to the room during processing. Contamination levels on
near-by radwaste equipment were as high as 200 mrad/hour. The
general area surfaces in the truck bay were contaminated up to 30,000
dpm/100cm (2)" (NRC IR 50-277/92-12 and 50-278/92-12.)
May 4, 1992 - Philadelphia Electric "initiated a planned shutdown
[at Unit 3] in order to repair a large steam leak through a manway on the
'F' moisture separator tank" (NRC inspections 50-277/92-11 and 50-
278/92-11.)
May 12, 1992 - Unit 3 recirculation pump trip occurred at 80%
power.(See June 27, July 23, July 26 and July 27, 1992 for related
incidents.)
May 15, 1992 - PECO initiated a shutdown of Unit 2 "due to
inoperability of the high pressure coolant injection and the reactor core
isolation cooling systems" (NRC inspections 50-277/92-11 and 50-278/92-
11.) (See June 25, 1992 for related incident.)
May 20, 1992 - Unit 2 experienced a reactor scram and turbine
trip due to a malfunctioning combined intermediate valve.
May 22, 1992 - The motor for the Unit 3 residual heat removal
pump failed and was declared inoperable.
June 1, 1992 - "Common stock earnings for the first quarter of
1992 were $0.33 per share, $0.25 lower than the $0.58 per share
earnings for the corresponding period last year. The reduction in earnings
was primarily the result of the previously reported settlement of litigation
by the co-owners of Peach Bottom Atomic Power Station which reduced
first quarter earnings by approximately $0.27 per share" (J.F. Paquette,
Jr., Chairman of the Board and Chief Executive Officer, Report to
Shareholders First Quarter, 1992).
June 25, 1992 - The Unit 3 high pressure coolant injection system
was declared inoperable "due to excessive water buildup in the turbine
casing" (NRC IR 50-277/92-13 and 50-278/92-13.) (See May 15, 1992 for
a related incident.)
June 27, 1992 - The 'A' recirculation pump tripped at Unit 2.(See
May 12, July 23, July 26 and 27, 1992 for related incidents.)
July 4, 1992 - An Alert was declared at Peach Bottom due an
explosion at the #1 transformer station. Units 2 and 3 were operating at
at, or around, 95 % power. As a result of the explosion, Unit 3 scrammed
and there were several emergency safeguard actuations.(See May 2, 1991
for a related incident.)
July 14, 1992 - "Unit 3 was manually scrammed from 63% power
due to a decreasing main condenser vacuum" (NRC IR50-277/92-13 and
50-278/92-13.)
July 17, 1992 - Unit 2 experienced a turbine trip and reactor
scram at 95% power during a severe lightning storm.
July 23, 1992 - The Unit 3 recirculation pump tripped at 95%
power.(See May 12, June 27, July 26 and July 27, 1992 for related
incidents.)
July 25, 1992 - "Unit 2 was shutdown due to a safety relief valve
bellows rupture alarm" (NRC IR 50-277/92-13 and 50-278/92-13.)
July 26, 1992 - The 'A' recirculation pump tripped at Unit 2. (See
May 12, June 27, July 23 and July 27, 1992 for related incidents.)
July 26, 1992 - A safety device used at Peach Bottom and 35 other
American nuclear reactors may be defective according to the NRC.
"Engineers are concerned that in a serious accident involving the rapid
loss of coolant and pressure from the reactor, the device would give a false
reading, indicating the reactor core was still covered with water when it
actually was not and therefore in danger of melting down" ( Sunday
Patriot News, July 26, 1992 A3.) (See September 11, 1990 and March 26
and 27, 1992 for related incidents.)
Peach Bottom has had a history of problems in this area.
" In August 1990, the licensee identified that the Unit 2 level
instrumentation served by the 2B condensing chamber and reference leg
was indicating values about 11 inches higher than similar instruments
served by the 2A condensing chamber...They [PECO] concluded that the
actuation set points for several safety systems would be exceeded during
transients or accidents, declared the instruments inoperable and
completed a plant shutdown. Following the 1990 event, the licensee
revised the channel check procedures to provide better monitoring and
evaluation of the instruments...A second level offset event, again
Continued on the next page...
involving the Unit 2B condensing chamber, occurred in March 1992. The
improved surveillance procedures helped the licensee identify the offset
before it had exceeded 3 inches. In response, the licensee established a 4
1/2 inch offset operability limit, and closely monitored the
instrumentation..." (NRC IR 50-277/92-16 and 50-278/92-16.) ( For
related incidents see September 11, 1990 and March 26-27, 1992.)
July 27, 1992 - The 'A' recirculation pump tripped at Unit 2.
(See May 12, June 27, July 23 and July 26, 1992 for related
incidents.)
July 27, 1992 - Peach Bottom and 86 other suspected nuclear
reactors "depend on a defective and dangerous fire-barrier system
to protect electrical cables used for a safe shutdown during a
fire/accident." (Nuclear Information and Resource Service (NIRS), July
27, 1992.) The company who produces the Thermo-Lag 330 system is
Thermal Science, Inc. (TSI), St. Louis, Missouri. Among the problems with
Thermo-Lag are: combustibility, toxicity, seismic qualification,
vulnerability to water, incomplete installation and ampacity calculation
errors.
In an IR issued on September 10, 1992, PECO requested a temporary
waiver of technical specification compliance for certain fire barriers. The
NRC observed: "...the licensee could not post the required fire watch for
residual heat removal system cables running through the Unit 3 offgas
pipe tunnel because it is a high radiation area".
(NRC IR 5 277/92\16 and 50-278/92-16.)
August 6, 1992 - The NRC issued a violation "for operation of the
reactor cleanup system in a mode not established in approved operating
procedures, is of concern because it represents a weakness in your control
of operating activities" (NRC IR 50-277/92-13 and 50-278/92-13.)
August 10, 1992 - PECO entered a seven day maintenance outage on
the E-4 emergency diesel generator.
August 17, 1992 - A generator lock-out and reactor scram occurred at
Unit 2 due to improper blocking. PECO "determined that the generator
lock-out occurred because the permit being applied in the South Substation
was incorrect" (NRC IR 50-277/92-16 and 50-278/92-16.)
August 20, 1992 - The Unit 3 Emergency Core Coolant System power
supply failed. The root cause was a failed topaz inverter.
September 14, 1992 - A licensed operator tested positive for
marijuana use.
October 6, 1992 - During an NRC inspection relating to plant
security, one unresolved Fitness-for-Duty(FFD) item was identified. The
NRC also cautioned that "... additional attention is warranted on the
effectiveness of routine security patrols since we identified certain
deficiencies during this inspection that should have been identified by
your officers on patrol" (NRC IR 50-277/92-20 and 50-278/92-20.)
October 15, 1992 - Unit 3 scrammed and the high pressure coolant
injection (HPCI) system initiated: "... Unit 3 experienced a primary
containment isolation system (PCIS) group I isolation on main steam line
(MSL) low pressure. This resulted in closure of the MSIVs and a reactor
scram. During the post-scram pressure and level transient, vessel water
decreased to the ECCS Lo Level initiation setpoint. The high pressure
coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems
initiated and injected into the reactor vessel. The alternate rod insertion
and reactor recirculation point trip logic also actuated. Three main steam
safety relief valves (SRV) opened automatically for a short period to
control pressure, and later re-closed. The licensee declared an unusual
event (UE) at about 9:25 p.m. due to the initiation and ejection of an
ECCS system in response to a valid signal...At about 11;16 p.m., while
proceeding with the plant cooldown, reactor vessel level increased above
the normal operating band and caused a HPCI and RCIC high reactor
vessel water level turbine trip. Due to the temporary loss of HPCI as a
means of pressure control, reactor pressure increased to the high pressure
scram setpoint. the operators manually operated an SRV to reduce
pressure, and restarted HPCI and RCIC. the licensee also reported this
second scram signal to the NRC via the ENS. All systems responded as
expected following the PCIS group I isolation and reactor scram, and the
subsequent high reactor pressure scram" (NRC IR 50-277/92-27 and 50-
278/92-27.)
PECO management decided to shut the plant for five days.
After reviewing the events the NRC issued a Notice of Violation and
criticized, "The control room staff did not effectively monitor developing
reactor coolant stratification following the Unit 3 automatic scram, and
certain Technical Specification reactor pressure/temperature limits were
exceeded. Adequate controls were not in place to ensure that the transient
was appropriately evaluated before plant restart. Also, operators did not
record required pressure data used to evaluate compliance with
pressure/temperature limits following a Unit 2 shut-down." (E.
Wenzinger, Chief, Projects Branch 2, Division of Reactor Projects,
November 16, 1992.)
October 16, 1992 - The NRC found one potential problem with senior
reactor operators (SRO) examinations:"Since SRO Upgrades are currently
licensed individuals at your facility, we are concerned that your training
program may not be emphasizing a high level of performance among
reactor operators in referring to and using procedures" (NRC IR 50-
277/92-18 and 50-278/92-18.)
October 15, 1992 - Unit-3 scrammed and recirculation pumps shutdown,
“there was a significant cool down in the bottom head as a result of the loss of
forced circulation” (IR 50-277/94-04 and 50-278/94-04.)
October 16, 1992 - The NRC identified programmatic weaknesses related
to the System Manager program. (NRC IR 50-277/92-26 and 50-278/92-26.)
November 16, 1992 - The NRC noted: “An industrial safety concern,
which involved the potential for loss of power in the drywell...had not yet been
resolved and warrants your attention” (NRC IR 50-277/92-30 and 50-278/92-
30.) (See December 12, 1995 for a related incident.)
December 2 and 11, 1992 - Failures of the containment, atmospheric,
dilution (CAD) system gas analyzer occurred at Unit-2. On both occasions PECO
personnel did not “understand” or “recognize” the problem with the CAD. (NRC
IR 50-277/92-29 and 50-278/92-29.)
December 4, 1992 - Several weaknesses were reported during the the
Initial SALP of Licensee Performance “including numerous component failures,
lapses in the operating procedure and deficiencies in engineering and technical
support” (York Daily Record, January 9, 1993.) “Among the areas identified for
improvement were plant performance monitoring and engineering and
technical support” (PECO, Report to the Shar eholde r s, March 1, 1993.)
December 7, 1992 - During Unit-2 start-up, the ‘2B’ Recirculation Pump
failed. (NRC IR 50-277/92-32 and 50-278/92-32.) (See March 2, 1993 for a
related incident.)
December 17, 1992 - Turbine control oscillations occurred while Unit-2
was operating at 89.5% power. The plant was “stabilized” at 76.5% power. (NRC
IR 50-277/92-32 and 50-278/92-32.)
December 19, 1992 - An Unusual Event was declared “due to a loss of
emergency communications capabilities. Both units were operating at 20%
power” (NRC IR 50-277/92-32 and 50-278/92-32.)
January 1, 1993 - The Unit-2 high pressure coolant injection system was
declared inoperable. (NRC IR 50-277/92-32 and 50-278/92-32.) (See January
25 and 31, March 1 and August 9, 1993, for related incidents.)- January 21, 1993 - A Notice of Violation (NOV) was issued relating to the
NRC’s Motor-Operated Valve (MOV) Inspection on October 19-23 and November
3, 1992. PECO “1) did not document nonconforming positions, 2) did not
properly disposition existing nonconforming conditions, and 3) did not take
timely corrective actions to evaluate and resolve nonconforming conditions in
MOVs...” (NRC IR 50-277/92-82; 50-278/92-82.) (See August 8-16, 1998, for a
related incident.)
January 25, 1993 - During surveillance testing, the Unit-3 high
pressure coolant injection system was declared inoperable. (NRC IR 50-277/93-
01 and 50-278/93-01.) (See January 1 and 31, March 1 and August 9, 1993, for
related incidents.)
January 31, 1993 - The Unit-2 high pressure coolant injection system
was declared inoperable. (NRC IR 50-277/93-01 and 50-278/93-01.) (See
January 1 and 25, March 1, and August 9, 1993, for related incidents.)
March 2, 1993 - Unit-2 scrammed while operating at 70% reactor power.
(NRC IR 50-277/93-03 and 50-278/93-03.)
March 2, 1993 - The Unit-2 ‘2A’ reactor recirculation pump and ‘2A’
condensate pump tripped while the Unit was operating at 100% power” (NRC IR
50-277/93-03 and 50-278/93-03.) (See December 7, 1992 for a related
i n c i d e n t . )
March 3, 1993 - The Unit-2 high pressure coolant injection system was
declared inoperable. (NRC IR 50-277/93-03 and 50-278/93-01.) (See January
1, 25 and 31 and August 9, 1993 for related incidents.)
March 7, 1993 - [R]eactor scram, due to a low reactor vessel level.
Reactor feed pump trip while lowering reactor power to with in bypass valve
capacity, to allow work on turbine valves” (IR 50-277/94-04 and 50-278/94-
0 4 . )
March 10, 1993 - During a radiological safety inspection (February 8-9,
1993 and March 1-2, 1993), relating to a “breakdown of personnel access
controls associated with the Transversing In-core Probe (TIP), the NRC found:
“...control of personnel during such operations is considered very important as
the TIPs represent one of the higher radiation sources that personnel have a
potential for encountering” (NRC IR 50-277/93-02; 50-278/93-02.) (For related
incidents see June 22 and 25, September 24, October 4, and November 11,
1993; June 19 and November 29, 1994 and August 24, 1995.)
March 23, 1993 - High oxygen concentration was found in Unit- 2
containment during power operation. (NRC IR 50-277/93-03 and 50-278/93-
03.) (See January 17, 1992 for a related incident.)- April 24, 1993 - Unit-2 was manually scrammed “following declaration
of all reactor vessel level instrumentation served by the ‘2B’ condensing
chamber inoperable” (NRC IR 50-277/93-06 and 50-278/93-06.) (See related
incident on March 27 and July 26, 1992 and September 22, 1993.)
April 30, 1993 - A Notice of Violation was issued following an an NRC
inspection of the electrical distribution system. Other design and operational
weaknesses were identified relating to the emergency diesel generator. (NRC IR
50-277/93-80 and 50-278/93-80.) (See July 17, 1995 for a related
d e v e l o pme n t . )
May 26, 1993 - Three individuals were found to be “inattentive” or
“sleeping.” (C. Anderson, NRC Region I.)
June 22, 1993 - “Controls over a special high radiation area entry were
not fully effective in that a higher than expected dose rate was identified upon
the entry” (IR 50-277/94-04 and 50-278/94-04.) (See March 10, June 25,
September 24 and October 4 and November 11, 1993 and January 19 and
November 29, 1994.)
June 24, 1993 - PECO discovered a “mispositioned” control rod at Unit-2.
The reactor was operating at 60% power. (NRC IR 50-277/93-15 and 50-
278/93-15.) (For related events see February 22, 1994, April 21, 1995 and
February 15, 1997.)
June 25, 1993 “[U]unlock[ed] high radiation area door” (IR 50-277/94-
04 and 50-278/94-04.) (See March 10, June 22, July 22, September 24,
October 4 and November 11,1993 and January 19 and November 29, 1994.)
July 4, 1993 - Unit 3 was shutdown. “An unplanned Unit 3 mid-cycle
outage began on July 6, 1993, to replace to known leaking fuel bundles.” A fuel
leak was detected in May 1992. (NRC IR 50-277/93-15 and 50-278/93-15.)
July 30, 1993 - Unit-3 was manually scrammed “after a loss of
condenser vacuum” (NRC IR 50-277/93-15 and 50-278/93-15.)
August 9, 1993 - The Unit-3 high pressure injection system was rendered
inoperable (NRC IR 50-277/93-17 and 50-278/93-17.) (For related incidents
see, January 1, 25 and 31 and March 1, 1993.)
August 11, 1993 - Unit-2 was manually scrammed. (NRC IR 50-277/93-
17 and 50-278/93-17.)
August 14, 1993 - Unit-3 was shut down after three of four residual heat
pumps were deemed inoperable. The plant was operating at 100% power. (NRC
IR 50-277/93-17 and 50-278/93-17.)- September 14, 1993 - The reactor feed pump tripped due to “flow
oscillations” at Unit-3.
September 16, 1993 - An inspection of Peach Bottom’s Emergency
preparedness program on June 28-30, 1993 found: “Significant areas for
potential improvement included wind direction information use by emergency
response groups, event announcements in the Emergency Operations Facility by
the ERM [Emergency Response Manager], and ERM recognition of the best
indication of main stack radiation” (NRC IR 50-277/93-10; 50-278/93-10.)
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