Microsoft Word 102210-1 Loss of Cogen Final doc



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2010-1022-ii-report
INVESTIGATION TEAM
The team members were ME&I Superintendent (Leader, Senior Process Engineer, SPP Operator, Marine Terminal Dispatcher (JHSC member, and HS Special Projects Coordinator (TapRooT® Facilitator.

ATTACHMENTS

1. TapRoot® SnapChart
2. Event Summary – October 22, 2010 3. Steam System Event Summary – October 22, 2010 4. Plant Instrumentation Trend Charts


ConocoPhillips Company

12

Loss of Cogeneration Units 102210-1 #144138
ATTACHMENT 1


ConocoPhillips Company
Loss of Cogeneration Units 102210-1 #144138

13 10/22/2010 10:43 AM
Air Liquide (AL)
Shutdown
About 10/22/2010 11:00 AM
Shift Supt
Implemented
Steam Curtailment
Procedure
10/22/2010 10:44 AM
SPP G23A
Shutdown
10/22/2010 11:03 AM
GB301 Air
Compressor
Shutdown
105 MMSCFD of hydrogen to refinery MLB/Hr of steam to refinery
REOP-2
Low Steam
Pressure
AL at high rate of production
Trip due to High
Basket temperature
SD within seconds of fuel pressure increase control circuits inadequate to control 20 PSIG Fuel gas increase
SPP BC Triconex handled fuel gas pressure surge of PSIG
600# Steam at
400#
Air system lost but holding with electric compressors in service
A
Second SD at high rate AL SD & 5 rate reductions
[9/26/09-10/22/10]
About U Plant 4 is shutdown and steam rate increases during st minutes
Fuel gas pressure increased 20 PSIG
Loss of COGEN Units 102210-1
IMP#144138


ConocoPhillips Company
Loss of Cogeneration Units 102210-1 #144138

14


ConocoPhillips Company
Loss of Cogeneration Units 102210-1 #144138

15 10/22/2010 2:27 PM
SPP GT23B
shutdown
Loss of SPP
Instrument Air 2:12 PM
SPP GT23C
shutdown
Refinery Flare begins to smoke 2:37 PM
CWS Level 2
Flameout
SPP is now at
One Gas Turbine in Operation 3:05 PM
U240 plant
Depressurizing to
Flare 100 PSI/min
Condensate swept into
GT23C
600# Steam dropping 18
PSI/min [285#]
SPP Instrument
Air drops 75# in min
Poor Firing control low air pressure
SD on high basket temperature
SFR Total Steam
Failure 600# at 150# at B 2:11 AM
Steam Injection Air
Purge Activated
GT23B has
500lb/HR leakage on steam injection line- no condensate Steam sytem pressure <560#
triggers air purge
Excessive air leakage into
GT23C?
Insufficient steam to operate
Media attention


ConocoPhillips Company

16

Loss of Cogeneration Units 102210-1 #144138

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