February 26, 2002 - Corbin McNeill Jr. announced his retirement, and
he is expected to receive $7 million when leaves the Company in April, 2002. He
will also receive a bonus payment. McNeill made $2.5 million in 2001.*
“His severance equals triple the sum of his annual base salary plus the
average of his bonus over the last two years.
“McNeill is the company’s largest individual shareholder. His 1.53 million
shares are worth $79.1 million based on yesterday’s closing price of $51.70.”
(Philadelphia Inquirer, C-1, March 14, 2002.)* Corbin A. McNeill’s base salary, after the merger increased, from
$659,857 to $855,830, and his bonus was increased from $1 million to
$1,081,572. In addition, McNeill's restricted stock increased from $942,188 to
$2.8 million. [May 20, 2001.]
(See June 13 and September 28, October 24 & December 21, 2001, for
information on 900 job cuts, and refer to January 29, 2002, for further job
cuts. ”)
March 28, 2002 - The NRC admitted that Peach Bottom and the 102
nuclear power plants could not withstand an impact of airplane the size of those
that crashed into the Pentagon and World Trade Center on September 11, 2001.
(March 28, 2002, Patriot News.) (See October 2001 & October 17, 2001 and
January, 9 and 30, 2002, for related incidents.)
April 3, 2002 - “Two men and a male juvenile from Mexico face possible
deportation after attempting to enter an unprotected area of the Peach Bottom
Atomic Power Station. All three remained in INS custody Wednesday.”(York
Daily Record, April 4, 2002.) (See January, 2001, October 6, 2001 & October
17, January, 9 and 30, 2002, and March 21 and May 15, 2002, for related
inc ident s . )
April 17, 2002 - Exelon Corp., the country's largest nuclear plant
operator, said yesterday that it would end its bid to develop the next generation
of nuclear reactors.
The Chicago-based parent of Peco Energy Co. said it would terminate its
nearly two-year relationship with Eskom, South Africa's state-owned utility, in
building a prototype gas-cooled reactor. Exelon is getting out of the business of
designing nuclear plants and will concentrate instead on operating them.
The company spent $20 million on the project, of which it owned 12.5
percent. Exelon said it already had paid for its share as a research-anddevelopment expense. It has not decided what to do with the 12 employees it had
working on the project, a spokeswoman said. (Benjamin Y. Lowe, Philadelphia
Inqui r e r, April 17, 2002.) (See December 5 & 10, 2001, for background
i n f o rma t i o n . )
April 22, 2002 - Exelon's 1st-Quarter Net Income Fell 98%
... as mild winter weather and maintenance costs hurt results.
“The country's largest operator of nuclear power plants reported late
Monday net income of $8 million, or two cents a share, compared with net
income of $399 million, or $1.23 a share, a year earlier.
“The latest results included a charge of $230 million, or 71 cents a share,
from the effect of adopting SFAS 142 for goodwill amortization, while year-
earlier results included a tax benefit for the implementation of SFAS 143 for
derivatives. Excluding these items, the company said it had operating earnings
of 77 cents a share, compared with operating earnings of $387 million, or $1.19
a share.” (Mon Apr 22,10:53 PM ET , CHICAGO -- Exelon Corp. )
(See June 13 and September 28, October 24 & December 21, 2001; and,
January 29 & February 26, 2002. For information related economic
de v e lopment s . )
May 11, 2002- “Exelon Corp. is the subject of a shareholder lawsuit
alleging the electric and gas utility made false and misleading statements that
artificially inflated its share price. The law firm of Charles J. Piven said it filed a
lawsuit on behalf of buyers of Exelon shares between April 24, 2001, and
September 27.” (Philadelphia Inquirer, D-3, May 11, 2002.)
May 15, 2002 - “A foreign intelligence service recently warned that a
nuclear power plant in the Northeast could be the target of a July 4 terrorist
attack...Published reports suggested that the target could be Pennsylvania’s
Three Mile Island, but a second US official with knowledge of the information said
no specific facility had been named.” (Knight Ridder, May 15, 2002.) (See
January, 2001, October 6, 2001 & October 17, January, 9 and 30, 2002, and
March 21, for related incidents.)
May 28, 2002 - “Exelon Corp. and three other utilities [Main Yankee
Atomic Power Co., Omaha Public Power District & Sacramento Municipal Utility
District] lost a $2.2 billion legal challenge to the federal government’s nuclearwaste cleanup plan...In 1992, Congress ordered utility companies that use
government uranium-enrichment services to pay one-third of the cleanup bill.
The U.S. Supreme Court said yesterday that it would not hear an appeals from
the companies that argue that the assessments are unconstitutional.”
(“Associated Press”, May 29, 2002.)
June 2, 2002 -An alert began at around 12:30 am, ending at 3:01 am,
relating to the activation of the fire suppression system due to EDG failure which
released carbon dioxide into a room where two employees were working. No
injuries were reported and both Peach Bottom 2 & 3 remained at 100% power.
(Exelon Nuclear, News Release, June 2, 2002, 4:10 am.) (See November 26,
2002 for follow-up, and July 11, 2003 for absolution.)
June 12, 2002 - The Bioterrorism Bill signed into law on June 12, 2002
mandates KI stockpiles out to 20 miles.
June 25, 2002 - “...station emergency preparedness personnel discovered
that the emergency planning siren base station at the site, was unable to
communicate with the off site sirens, due to external radio frequency noise in the
area.” (IR-50-277/02-05; 50-278/02-05)
July 1, 2002 - The NRC found that on February 12, 2002, Exelon “did
not identify that key information needed by the emergency director (ED) to
classify the simulated event as a General Emergency was not provided to the ED
by members of the Emergency Response Organization (ERO). The finding was
preliminary classified as White because the critique failed to identify a problem
associated with the implementation of a risk significant planning standard.”
...Continued on the following page...Exelon disputed the findings on September 4, 2002.
The NRC reasserted that “the critique problems were more than minor but
the Issuance of the White finding is not appropriate because the inadequate
critique did not result in a failure to identify a risk significant planning standard
(RSPS) problem.”
The incident is classified a Non-Cited Violation.
(Final Significance Determination for Green and White Findings and a Notice
of Violation at Peach Bottom, IR-50-277/02-07; 50-278/02-07).
This was the twenty-fifth Non-Cited Violation since June 1998. Exelon's
total cost avoidance, i.e., “credit” for 25 Non-Cited Violations = $1 ,255,000.
July 21, 2002- At Unit-2, “the fifth stage feed water heaters were
removed from service for end-of-cycle coast down.” (IR-50-277/02-05; 50-
278/02-05). (See August 4, 2002 for related event.)
July 23, 2002- “Exelon did not evaluate in a prompt manner whether it
was appropriate to disable the electrical trips of the EDGs from the cardox
injection fire protections system after NRC inspectors identified that the trips
were still active with the EDG cardox system isolated” (IR-50-277/03-02; 50-
278/03-02) (Also refer to IR-50-277/02-04; 50-278/02-04).
(See April 23, 2004 for NCV).
August 4, 2002- At Unit-2, “the fourth stage feed water heaters were
removed from service.” (IR-50-277/02-05; 50-278/02-05). (See July 21, 2002
for related event.)
August 15, 2002 - Despite a favorable EIS of Exelon’s request for a license
extension at Peach Bottom-2 & -3, the NRC listed three safety issues that need to
be addressed prior to approval: replacement o electric fuse clips; removal of the
anti-aging plan; and, replacement of faulty cables.
August 30, 2002- At Unit-3, “power was reduced to approximately 90%
prior to shut down the 3 ‘A’ recirculating water pump because of high
differential pressures on the circulating water intake screens. The high
differential pressures were caused by a sudden surge in the amount of fish
(Gizzard Shad) that entered the intake canal and clogged the screens. Unit 3
power was returned to 100 percent following cleaning of the circulating water
screens and restating of the 3’A’ circulating water pump.” (IR-50-277/02-05;
50-278/02-05).
August 31, 2002 - New security budget increased to $2.2 million
annually or $550,300 less than John W. Rowe’s base salary.- September 5, 2002 -- Three Mile Island Alert filed a formal Petition for
Rulemaking with the Nuclear Regulatory Commission to include day-care
centers and nursery schools in emergency evacuation planning. The proposed
rule would affect all 103 operating nuclear plants in the United States.
September 10, 2002 - The Office of Homeland Security announced that
the “yellow” warning had been increased to a heightened state of alert or an
“orange” upgrade at 1:00 pm. (Exelon Public Relations.)
- “...Unit 2 was manually scrammed, in preparation for the 2R14
refueling outage” (IR-50-277/02-05; 50-278/02-05).
November, 2002 - “ Governor Schweiker “directed the National Guard to
join State Police in a joint security mission at the state’s nuclear facilities.” In
December, the Governor extended the joint mission of the National Guard and
the State Police at the Commonwealth’s five nuclear generating stations until
March 4, 2002. (DEP, Update, December 6, 2002.)
September 21, 2002 - A Non Cited Violation was issued for incident
“when a chain broke” on a “rigging hoist and the motor, weighing
approximately 48,000 pounds, fell approximately ten inches into the
pump/motor stand.”
This was the twenty-sixth Non-Cited Violation since June 1998. Exelon's
total cost avoidance, i.e., “credit” for 26 Non-Cited Violations = $1 ,355,000.
November 26, 2002 - Initially classified as a White, the incident was
classified a Non-Cited Violation. (See June 2, 2002, for precursor event.)
(Final Significance Determination for Green and White Findings and a Notice of
Violation at Peach Bottom, IR-50-277/02-07; 50-278/02-07).
This was the twenty-seventh Non-Cited Violation since June 1998.
Exelon's total cost avoidance, i.e., “credit” for 27 Non-Cited Violations =
$1 ,355,000.
December 10, 2002 - A security challenge occurred at an Exelon nuclear
power plant outside of Chicago.
“BRAIDWOOD -- A crazed Chicagoan, swearing to be an extraterrestrial
alien, crashed his car through the gates of the Braidwood nuclear facility late
Monday before speeding away only to be arrested for reckless driving in
Wilmington minutes later.
...Continued on the following page... No injuries resulted. Metta said the intruder is alleged to have
penetrated the parking area by crashing through closed gates, flashing past a
plant checkpoint and then doing "donuts" in the parking lot. (“The Daily
Journal”, Kankakee IL.)” (See January 9 and December 20, 2002, for related
inc ident s . )
December 12, 2002 - TMI sirens malfunctioned in Cumberland and York
counties. In Dauphin County, 28 sirens malfunctioned due to the “inadvertent”
discharge of the “space bar” by a computer operator. (Refer to June 22, August
15 and October 5-9, 2001 and January 11, March 3 2002, for related
problems.)
December 20, 2002 - Another security challenge occurred at an Exelon
nuclear power plant outside of Chicago:
“BRAIDWOOD -- She was the second driver to breeze past the guard station
at Braidwood’s nuclear facility in the span of a week.
“But its unclear if the trespasses arrest of Wilmington’s Christina Staley,
Tuesday, will result in changes to the nuclear generating station’s security
apparatus.
“Neal Miller, station director, noted that Ms. Staley, 31, had apparently
become disoriented and was looking for some place to turn around when she
drove past the security at 9 a.m.”
(“The Daily Journal”, Kankakee IL.)”
(See January 9 and December 10, 2002, for related incidents.)
December 13, 2002 - A security challenge occurred at a nuclear facility
north of Peach Bottom, on the Susquehanna River
"At 1450 EST on 12/13/2002, Susquehanna LLC Main Control Room
received a request for additional information from the Pennsylvania Emergency
Management Agency (PEMA). PEMA received rumors that a HAZMAT team had
been dispatched to Susquehanna in response to a spill associated with a potential
sabotage event.
December 17, 2002 - “...Unit 2 power was reduced to approximately 16
percent to facilitate leak repairs on the Caldon LEFM flow measurement system.
After repairs, Unit 2 returned to 100 percent power in the afternoon of December
21” (IR 50-277/02-06; 50-278/02-06). (See April 30 - May 11, 2003, for a
similar problem).
December 21, 2002 - An LER was recorded after “Unit 2 automatically
shutdown from 100% power when the main steam isolation valves closed due to
a Group I Primary Containment Isolation System (PCIC) actuation” (IR 50-277-
03-02; IR-50-278/03-02). “For example, on Dec. 21, 2002, a Peach Bottom Atomic Power Station Unit 2 electro-hydrolic control system circuit card failure triggered a scram, according to the NRC’s report. That system controls the wide-range speed control of the turbine, Sheehan said.“In other words,” Sheehan said, “it serves as a sort of high-tech throttle for the plant’s turbine, thereby controlling the plant’s power output.”“On Dec. 22, 2004, the NRC report said, another part of that same system malfunctioned, causing a loss of reactor pressure and forcing a scram.” (“York Sunday News”, March 13, 2005)
January 28, 2003 - An NCV was issued relating to Exelon's failure to
correct and maintain “preventative maintenance activities and procedures on
critical, safety related ventilation dampers since 1988...A contributing cause to
the length of time that Exelon did not identify this issue was related to the
Problem Identification and Resolution crosscutting area. Peach Bottom plant
personnel did not identify the lack of preventative maintenance for safetyrelated dampers following the identification of excessive stroke times...in June
2000 or...failure to stroke on June 16, 2002” (IR 50-277-02-06; IR-50-278/02-
0 6 ) .
This was the twenty-eighth Non-Cited Violation since June 1998.
Exelon's total cost avoidance, i.e., “credit” for 28 Non-Cited Violations =
$1 ,405,000.
February 11, 2003 - A Severity Level IV violation was issued by the
NRC. Exelon made changes to their emergency plans without prior NRC
a p p r o v a l .
“The finding was determined to be more than minor as its significance was
related to the impact it would have on the mobilization of the emergency
response organization and preclude offsite agencies from being aware of adverse
conditions on site” (NCV 50-277; IR-50-278/03-006-01);
This Violation was classified a Non-Cited Violation. This was the twentyninth Non-Cited Violation since June 1998. Exelon's total cost avoidance,
i.e., “credi t” for 29 Non-Cited Violations = $1 ,455,000.
February 17, 2003 - PEACH BOTTOM-2 WAS REDUCED TO 45%
POWER AFTER A RECIRCULATION PUMP tripped. Exelon spokesman Dave
Simon said the trip occurred Feb. 17 at 6:48 a.m. The root cause of the trip has
not yet been determined, he added. Simon declined to say how long the unit is
expected to be operating at the reduced power level. Peach Bottom-2 was at full
power prior to incident (Reut e r s.) The plant ramped up to full power by February
20, 2003. Reuters: Exelon's Pa. Peach Bottom 2 nuke drops to 41 pct
Tuesday February 18, 8:25 am ET NEW YORK, Feb. 18 (Reuters) - Exelon Nuclear's 1,110 megawatt Peach Bottom 2 nuclear unit in Pennsylvania was at 41 percent power early Tuesday, down from full power on Friday, the U.S. Nuclear Regulatory Commission said in its power reactor status report. It was not immediately known why the unit, located in Delta, Pennsylvania, had been reduced. Meanwhile, the adjacent 1,110 MW Unit 3 continued to operate at full
power on Monday. The NRC did not issue a reactor status report on Monday due to the U.S. Presidents Day holiday. Exelon Nuclear is a unit of Exelon Corp. of Chicago.
April 12-15, 2003 - At Unit-2, “an automatic reactor shutdown occurred
due to high reactor pressure after the ‘D’ outboard main steam isolation valve
(MSIV) collapsed. The MSIV closes as a result of a failed instrument line valve.
Unit 2 returned to 100% power on April 15, 2003”. On April 12, 2003, “Unit 2 unexpectedly shut down when a single main steam isolation valve failed to close, based on a broken air-supply line. Exelon concluded that the valve’s air tubing was vulnerable to a fatigue failure.“While the plant did inspect more than 200 pneumatic lines linked to airoperated valves on both Unit 2 and Unit 3, the review did not take into account similar equipment such as instrument lines, according to the report” (“York Sunday News”, March 13, 2005.)- April 19, 2003 - A Green Non-Cited Violation was issued “when approximately 25 minutes into a planned load endurance test run for the E2 EDG, a small fire occurred on the EDG manifold” (IR 50-277-200-3003; IR-50-278/200-3003). This was the thirtieth Non-Cited Violation since June 1998. Exelon's total cost avoidance, i.e., “credit” for 30 Non-Cited Violations = $ 1 , 505 ,000.
April 23, 2003 - A Non-Cited Violation was issued for problems associated
with the EDG cardox system on July 23, 2002.
This was the thirty-first Non-Cited Violation since June 1998. Exelon's
total cost avoidance, i.e., “credi t” for 31 Non-Cited Violations = $1 ,555,000.
April 23, 2003 - A Non-Cited Violation was issued for problems associated
with emergency lighting units from November 6, 2002 through March 30,
2003. Eight-hour support batteries for three areas were not provided, i.e. Unit 2
RHR room, Unit 3 RHR room and Unit 3 RB “south isolation valve room.”
(IR 50-277-03-02; IR-50-278/03-02).
This was the thirty-second Non-Cited Violation since June 1998.
Exelon's total cost avoidance, i.e., “credit” for 32 Non-Cited Violations =
$1,610,000.
April 30 - May 11, 2003 - Unit-2 power “was reduced to approximately
30 percent to facilitate repairs to the Caldon leading edge flow meter (LEFM)
system and for power suppression testing, to identify a leaking fuel assembly.
During power ascension to approximately 85 percent, on May 6, following
repairs to the Caldon LEFM system and after the leaking fuel assembly was
identified and the adjacent control rod was inserted and de-energized, the #3
main turbine control valve started oscillating. Unit power was reduced to
approximately 40 percent to facilitate repairs to the main turbine control valve.
On May 11, 2003, Unit 2 returned to 10o percent power after the #3 main
turbine control valve was repaired” (IR 50-277-200-3003; IR-50-278/200-
3003). (See December 17, 2002, for a similar problem).
May 8, 2003 --The NRC RENEWED THE OPERATING LICENSES FOR
PEACH BOTTOM-2 AND -3 FOR AN additional 20 years, the agency said today.
The licenses will now expire on August 8, 2033 for unit 2 and July 2, 2034 for
unit 3. Exelon had submitted the license renewal application on July 2, 2001
(Platts, Nuclear News.)
May 8, 2003 --EXELON LOWERED POWER AT PEACH BOTTOM-2 TO FIX
A TURBINE CONTROL VALVE. The problem was discovered at around 3 p.m.
yesterday as the unit was powering back up following completion of power
suppression testing, company spokesman Dave Simon said. The unit had been
operating at around 61% since April 30 while the power suppression testing was
being conducted. It reached as high as 86% before being lowered to 42% to repair
the control valve. Simon declined to say how long the repairs would take or when
the unit would be returned to full power (Platts, Nuclear News. )
May 13, 2003 - During a surveillance test, technician discovered a “ wire
for the station power supply” was broken. (IR 50-277-03-02; IR-50-278/03-02).
This was the thirty-third Non-Cited Violation since June 1998. Exelon's
total cost avoidance, i.e., “credit” for 33 Non-Cited Violations =
$1,665,000.
SCRAM: APPENDIX "R" ISSUE AT PEACH BOTTOM 3
- "On May 14, 2003, at approximately 0410, the shift supervisor
determined that the Alternate Shutdown Panel on Unit 3 was not operable
following discovery of a de-energized power supply. The panel provides the
capability to maintain a safe shutdown path for a fire in the cable spreading
room, main control room or main control room fan room. Therefore, operators
would have been prevented from implementing required actions for a fire in
those areas. The apparent cause of the loss of power was a broken wire, which
was discovered during routine testing of the panel.
"Power was restored to the Alternate Shutdown Panel at approximately
1030 on May 14, 2003 and further investigation is in progress to determine the
cause of the broken wire and full extent and effect of the de-energization of the
panel." (U.S. Nuclear Regulatory Commission Operations Center,
Event Reports For 05/14/2003 - 05/15/2003.)
“Pa. Nuclear Operator Found Drunk on Job”
May 14, 2003 - An employee at two Pennsylvania nuclear power plants
has been suspended for being intoxicated on the job, according to a Nuclear
Regulatory Commission report. The employee tested positive as being under the influence of alcohol during a random May 14 drug test at the Limerick Generating Station, according to the report. The test was given at 9:45 a.m., when the employee had already been at work for several hours, the report stated.
...Continued on the following page...The employee had been licensed to operate reactors at the Limerick plant in Montgomery County and the Peach Bottom plant in York County before being suspended by Exelon Nuclear, officials said.
The NRC considers nuclear workers with a blood-alcohol content of 0.04 or
above to be intoxicated. The state of Pennsylvania considers drivers with a 0.10
reading to be intoxicated and unfit to drive. The NRC is considering whether to issue the company a violation for the incident or revoke the operator's license. (See November 14, 2003, for a related d e v e l o pme n t . )
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